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Soduim Graphite Reactor, Quarterly Progress Report, September-November 1953

Description: "For a central station reactor power plant of the sodium-graphite type, two designs have been investigated. The first operates as a converter using slightly enriched uranium fuel and produces 150 electrical megawatts. The second operates as a thermal breeder using a U233-Th alloy fuel and produces 300 electrical megawatts. Consideration has also been given to the problem associated with the design and operation of the Sodium Reactor Experiment. All work related to the plutonium plus power … more
Date: July 1, 1954
Creator: Inman, G. M.
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SRE Fuel Element Damage: An Interim Report

Description: Abstract: During the course of power run 14 on the Sodium Reactor Experiment (SRE) at low power, the temperature difference among various fuel channels was found to be undesirably high. Normal operating practices did not succeed in reducing this temperature difference to acceptable values and on July 26, 1959, the run was terminated.
Date: November 30, 1959
Creator: Jarrett, A. A.
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SRE Mark II Fuel Handling Machine

Description: Abstract: The Sodium Reactor Experiment Mark II Fuel Handling Machine has been modified to ensure fuel and gas containment during core III operation. A new fuel control system has been designed for the fuel handling machine.
Date: April 20, 1965
Creator: Dietz, H. B.
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Study of SCTI Control System

Description: Introduction: This report has been prepared to document the extensive analytical work required to design the control system for the Sodium Components Test Installation (SCTI), constructed for the Atomic Energy Commission at the Atomics International field laboratory.
Date: December 1, 1964
Creator: Griffin, C. W.
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Terminal Status Report for the Processing Refabrication Experiment

Description: Introduction: A low-capacity, low-decontamination plant can be built, as part of a power reactor complex, to avoid long distance transfer of fuel to a high-capacity aqueous processing plant. Activation of such a complex, with the processing plant adjacent to the reactor it serves, could decrease the cost of the integrated fuel cycle. The study of this concept is a major objective of the Processing Refabrication Experiment (PRE).
Date: November 15, 1959
Creator: Sinizer, D. I.; Mattern, K. L. & Kendall, E. G.
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Thermal Cycling Tests of Porous Uranium

Description: Abstract: It has been proposed that a fuel element containing porous uranium be used for moderately high temperature applications. In an effort to determine the structural integrity of this type of fuel body, thermal cycling tests have been conducted on porous uranium.
Date: March 15, 1960
Creator: Wilkinson, L. E.
open access

U-10 Wt % Mo Fuel Element: Irradiation in SRE

Description: From abstract: The fuel element assembly was successfully irradiated in the SRE to a maximum burnup of 5300 Mwd/MTU, at a peak fission rate of approximately 1.5 x 10E13 fissions/cm3-sec and a maximum central temperature near 1200F.
Date: August 31, 1965
Creator: Arnold, J. L.; Miller, K. J. & Peterson, R. M.
open access

UC Fuel Element Design and Fabrication

Description: Abstract: Uranium monocarbide shows considerable potential for use as a fuel in high temperature, high power density, nuclear power reactors. As Atomics International is proposing its use in sodium graphite type reactors, it was necessary to develop a process for fabricaing sodium bonded uranium carbide fuel elements.
Date: August 1, 1964
Creator: Draganchuk, W.
open access

Uranium Production Reactor (UPR) Quarterly Progress Report, May-July, 1953

Description: "Measurements of the intra-cell neutron flux distributing for a proposed Uranium Production Reactor have been made using a mock-up of a portion of the reactor core. Thermal neutron and thorium resonance neutron flux-distributions were investigated. As a result of the experimental measurements on the first mock-up, a decrease in thorium content appeared necessary in the reactor design studies. Experiments are now in progress on a second mock-up in which this change has been made."
Date: March 15, 1954
Creator: Laubenstein, R. A.; Houghton, W. J. & Martin, D. H.
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