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Performance of the 19XB 10-Stage Axial-Flow Compressor

Description: The 19xB compressor, which replaces the 19B compressor and has the same length and diameter 88 the 19B compressor, was designed with 10 stages to deliver 30 pounds of air per second for a pressure ratio of 4.17 at an equivalent speed of 17,000 rpm; the 19B was designed with six stages for a pressure ratio of 2.7 at the same weight flow and speed as the 19XB compressor. The performance characteristics of the new compressor were determined at the NACA Cleveland laboratory at the request of the Bu… more
Date: December 30, 1946
Creator: Downing, Richard M. & Finger, Harold B.
Partner: UNT Libraries Government Documents Department
open access

Preliminary Tests of a Buffet Stall-Warning Device on a 1/5-Scale Model of the Republic XP-84 Airplane

Description: "During the first flight tests of the Republic XP-84 airplane it was discovered that there was a complete lack of stall warning. A short series of development tests of a suitable stall-warning device for the airplane was therefore made on a 1/5-scale model in the Langley 300 MPH 7- by 10-foot tunnel. Two similar stall-warning devices, each designed to produce early root stall which would provide a buffet warning, were tested" (p. 1).
Date: October 30, 1946
Creator: Tucker, Warren A. & Comisarow, Paul
Partner: UNT Libraries Government Documents Department
open access

Evaluation of Gust and Draft Velocities from Flights of P-61C Airplanes within Thunderstorms: August 23, 1946 to September 4, 1946 at Orlando, Florida

Description: This report presents the results obtained from gust and draft velocity measurements within thunderstorms for the period August 23, 1946 to September 4, 1946 at Orlando, Florida. These data are summarized in tables I end II and are of the type presented in reference 1 for previous flights. In several of the surveys, indications of ambient air temperature were obtained from photo-observer records. These data are summarized in table III.
Date: January 30, 1946
Creator: Tolefson, H. B.
Partner: UNT Libraries Government Documents Department
open access

Free-Spinning-Tunnel Tests of a 1/18-Scale Model of the Fairchild XNQ-1 Airplane, TED No. NACA 2398

Description: :Spin tests have been performed in the Langley 20-foot free-spinning tunnel on a 1/18-scale model of the Fairchild XNQ-1 airplane. The spin and recovery characteristics of the model were determined for the normal gross-weight loading and for two variations from this loading - center of gravity moved rearward and relative mass distribution increased along the fuselage. These tests were performed for two vertical-tail plan forms. The investigation also included simulated pilot-escape tests and ru… more
Date: September 30, 1946
Creator: Daughtridge, Lee T., Jr.
Partner: UNT Libraries Government Documents Department
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